AN/PRC-9 Radio, Korea-Vietnam Artillery Band

AN/PRC-9 Artillery Band Radio out of the box

I was looking for an old, unrepairable radio to hide an Icom 880H Amateur radio in and found a perfect example. This radio would be period appropriate, being produced in the 50s and its even the Artillery type, good match for my 2-130th Field Artillery marked truck. I wanted unrepairable since I didn’t want to mess up a potentially good radio and ruin some history. I got this from http://fairradio.com/ Fair Radio Sales who took the time to dig up a salvage radio for me. I hope to get one of their repairable AN/PRC-9 radios soon as well, maybe an AN/GRR-5 too.

The M37 truck has an antenna, antenna mount, and working speaker on it, but no radio base, so I’ll have to come up with a way to mount the radio, but it will be neat to have a working radio as I am driving the truck.

The AN/PRC-8, 9, and 10 series of radios came in versions for Armor (AN/PRC-8), Artillery (AN/PRC-9), and Infantry (AN/PRC-10). AN/PRC stands for Army/Navy Portable Radio Communications. A good article describing the series can be found at http://www.n6cc.com/prc-10-infantry-radio/. As a signal officer, I am glad they abandoned the Armor/Artillery/Infantry versions, but it likely was a good way to make this set (more) portable given the technology of the time. It is quite a compact radio, surprisingly, the Icom 880H just fits in the battery case.

AN/PRC-9 guts

I asked for a salvage radio, and this example was quite corroded inside, thus not really salvageable; but this is what I wanted as it will just be a place to hide the Icom 880H. I will preserve the tune dial gearing which is still running smoothly, rewire the handmike to work with the Icom, and maybe try to repurpose the dials to change channels or volume control. The Icom 880H has a remote control head which can mount in the glovebox to be handy, but not visible.

POR-15 first coat

I have heard good things about POR-15 and I’ll try it on this radio. Topcoat will be OD Green. As I get the wiring and mounting worked out, I will post these details.

Restoration and Adaptation of AN/PRC-9 (August 2022)

POR-15 will be great, it is tough stuff, but I put it on too thick. One thin layer of it then OD green would have been sufficient. I did two, I’ll strip it and start over. The paint pen also isn’t going to work, partially because it flows to fast and is not crisp, but the thick layer of paint isn’t helping either. I am not sure how I will tackle the fine, crisp lines needed for the raised metal. Stencils for the original markings should be doable (ORG, CH, POINTER ADJUST labels), but the raised metal is going to be a challenge.

Enamel paint pen isn’t cutting it, you can see the paint filling in spaces between letters as well

The battery box will work great for the ID-880H, but sadly I’ll have to cut a hole somewhere for power, I/O, and ventilation. There is a handy stand built right into the battery box, two legs that swing out, that could be a good candidate for hiding a hole underneath. The battery box was beat up, but I was able to (slowly) coax it back into shape with a softwood lever.

Icom ID-880H on its future home

Painting, take two

Paint stripped (again)

POR-15 is difficult to strip, which means it’s tough and durable so that is ultimately good news. Modern stripper won’t remove it, but it does soften it enough to gently pick it off with and Exacto knife. Tedious be effective, just be cautious about gouging the surface of the metal.


Painting rehearsal

The local hobby store in Topeka (Dee and Me Hobbies) suggested paint on a piece of glass or something and press the paint on. It seems to work well, but glass seems too stiff causing paint not to apply, and standard rubber is too soft which causes paint to flow past the letter faces. I found a drill bit holder that looks to have promise, made of stiff rubber. I’m applying an even, thin coat of paint then pressing it on the letter faces. I’ll get some practice then try again.

Second Coat of Paint and Padding for 880H (September 2022)

Turned out much better with a very thin coat of paint. The letters are crisp and should be easier to paint. I cut an 1 1/2 in hole in the battery box where the 880H vent is to get warm air out of the setup. I used a Dremel to make the rough cut and a round file to finish. I’ll get a rubber gromet for the vent and the power connection. The foam is some stuff I had lying around, and it will work great. Not too hard to cut and will cushion the radio while getting bumped around as I am driving.

I found a very helpful person that has Icom microphone elements, which I will use rather than adapting the old carbon mic in the H-33 military mic. It should be straightforward to hook up since it will be an Icom element.

I hooked up the radio in the battery box and listened to the local NOAA weather station, it was slightly muffled, but not as bad as I thought. The truck has military speaker as well that I will hook this radio too, I should be able to hear even while driving with little issue.

Adapting Icom HM-133 handmike to H-33

I didn’t really think about it when I first thought this up but wiring this won’t be as simple as reconnecting wires around. The microphone and handset speaker isn’t the same between the HM-133 (Icom) and H-33 (mil). The circuitboard in the HM-133 provides some supporting electronics along with some voltage. The actual (tiny) microphone in the HM-133 isn’t labeled either, it surprised me to find how miniature the mic is compared with the H-33 carbon mic.

HM-133 Mic element is the small silver disc on the board just above and right of center
The HM-133 provides a number of services beyond simply being a handmike using a microprocessor

I have some choices to make in wiring this. I can convert the audio from the mic/handset speaker/radio to the original elements in the H-33 somehow, use modern mic/speakers in the H-33 and assemble an approximation of the supporting electronics, or just take the circuit board from the HM-133 and put that whole thing in the radio and feed the (modern) mic element from it. Finding information on the components is difficult, but I finally found a resource I can use to understand more clearly what I am doing. https://www.tinymicros.com/wiki/Icom_HM-133 has extensive notes and links to datasheets on the components, including the specific mic, a Hosiden KUB2823 Microphone, at least that looks correct. Now instead of guessing what needs what if I make some supporting electronics, I can do this accurately.

I did get a collection of scrap components from https://www.7000mic.com/, which gives me some great options, but I really need to dig into the datasheets of these components, understand what they need and can do, so I am not needlessly wasting these items.

The earpiece hopefully will be straightforward, there is a speaker jack in the back of the radio I can use to feed the military loudspeaker in the truck and the earphone in the H-33, although I will have to get specific about what is being output at this jack and what the two speakers expect. Interestingly, one of modern earpiece speaker elements I have fits perfectly in the spot the old mil element did.

If I do end up just using the whole circuitboard from the HM-133, there is plenty of room in the AN/PRC-9 body to fit, since the components have been cleared out it minus the freq dial and gearing which I will preserve to keep the appearance of an AN/PRC-9.

As a Signal officer, I know electricity and radio theory basics, but I never really had to dig too far down into determining what a schematic is telling me. My enlisted days after being a 13B cannoner, in my 25 series signaller time, I did tuning of 12 series radios but that was a long time ago and I didn’t really have to interpret schematics as much as just know what to look for and what components might need replaced. I soldered and turned pots alot, but never really dug into ~why~ the circuits were as they were. Modern radios lend themselves even less to this as they generally get repaired by board replacement, which I found right before I went to OCS in my last days in the electronics shop with the SINCGARS. I really need to dig down and understand clearly what I can and should do in hooking this up to get a good result.

Once I get the right combo and get it working I will detail how I got there, the notes and links at https://www.tinymicros.com/wiki/Icom_HM-98/HM-133_Internals should get me on the right path. I have quite alot of study ahead of me, even though I wasn’t expecting it, I am happy to learn about something I have been wanting to understand for many years, electronics.

Getting Started with Connections

Successful Mic to U77/U79 to radio handset speaker test

I found some old speakers that were trash and got the speaker cable from that. On the U77/U79 connector, pins A and B are the speaker, so I soldered those in, plugged in the cable, and got audio through. I have to test the PTT function on the radio and how to get the mic part through. PTT on this radio appears to be more than just a press switch, the HM-133 sends a bitstream to PTT then a bitstream to key off. There is a PTT on the schematic that may just be simple key on/off and I’ll have to test that, but I am not optimistic. If it does not, I’ll have to see the behavior of the HM-133 PTT and see how I can extend that.

Layout plan so far

Mapping the U77/U79 connector to the 880H RJ45 jack should be straightforward from a physical wire perspective, but what properly goes where will be another story. Up next will be testing behavior of PTT and mic to see what my options for extending those are.

H-33 Military Handmike

H-33 Handmike disassembled

This mic has been confusing me for a bit, I really didn’t want to totally disassemble it, but continuity checks were not agreeing with documents I have found.

From H-33 Handset (prc68.com)

If I am to use the HM-133 circuitboard, I will need two wires for speaker, two wires for mic, and two wires for PTT. In testing the PTT from the HM-133, its a simple push switch so I can just loop in the H-33 PTT (F and H, brown and yellow), but the brown cable didn’t pass continuity. I exposed the wires on the H-33 and connected at the end of the brown on each side and found that if I flex the coiled wire, I get connection sometimes – meaning the cable itself is shot internally. Since I purchased this as a non-working display piece, this is fine/expected but I’ll have to get a replacement coiled wire or simply use another H-33. At least I got to see the U77 connector disassembled, which is surprisingly easier than I anticipated.

My current plan is to use A/B for speaker, C/D for mic, and F/H for PTT. My simple RadioShack soldering iron that I have had for decades really isn’t sufficient for this (tip to large and burned up), so I got a better Weller iron. I really wanted a Weller 1010 but went with the consumer 30w version for a third as much and it will do what I need done. I also found an assortment pack of diodes, resistors, capacitors, LEDs, and breadboard since I really need to get better with electronics. I need to be more like Sayid from Lost – he could build radios from junk like all signal officers should be able to.

MacGyver but with electronics

October Progress

Painted Radio Face

Painting the raised letters and getting an acceptable result was a challenge, but I was able to accomplish this using the stiff rubber drill bit holder (any flat piece of stiff rubber with just a little give would work) and painting this while holding it upside down. I used an Exacto to gently scrape paint the flowed/wicked despite being upside down. I would guess there is a better technique out there, but I couldn’t find it and I ended up with a decent result. The tuning knob works to move the frequency dial even if this isn’t connected to anything. Ill place an LED where the incandescent bulb was to illuminate the dial like the original.

U79 Connector Disassembled

The PTT problem was difficult to overcome, but I think I have it nailed. The U79 had oil in it to free the pins and this appeared to be just conductive enough to trigger the very sensitive HM-133 PTT circuit. Disassembly of the U79 as easier than I thought, and after cleaning it, the U79 no longer triggers the HM-133 PTT. The H-33 PTT still does trigger the HM-133, even after detailed cleaning. I was able to overcome this with a photo coupler – test rig below:

Opto Coupler Test Rig

I bought an assortment of electronic components and it had a photo sensitive resistor and LEDs, so I hooked the H-33 PTT to light and LED and the HM-133 on the photo resistor. This worked reliably and I was able to make a test call on 2m using the H-33 fully set up. I will order a PC817 Optocoupler for the final assembly. With the last technical issues out of the way, I can work on final assembly and get it in service.

Finishing up

Finished and tested

The radio is complete. The photo coupler solves the touchy HM-133 PTT problem reliably. I did put some electrical tape over the contacts in the mil H-33 PTT as it seemed to cause the LEDs to flicker sometimes without it, likely since they are slightly compressed when assembled and the connector leads are very close together. 10 Ohm resistors used to bring the buck delivered voltage down a bit from the top edge of the LED specifications. Talked to someone on 2m that stated my audio was good, so this setup seems complete electrically.

Layout Diagram
Foam Cut to House Buck and HM-133 Circuit board
Circuit Diagram (from http://falstad.com/)

Now that it is complete, I will post the details in a separate post since this post was long and has some wrong turns in it. I also have to stencil on the ORG/CH table that was on the original to be completely done, but this will go nicely with the M37 when it is finished. Most photos of the M37 with a radio shows it mounted in the bed area, but I would like this radio in the cab. Hopefully I can find a photo of such a setup.

Cost of Dodge M37 rear main oil seal repair (by rebuilding everything)

My engine suffered a broken crankshaft and broken piston. Not bad after nearly 70 years. I knew that a rebuild would be needed at some point and wondered how much this would cost. Now that I am doing an engine/transmission rebuild, I (will) have the answer.

All parts came from the very helpful staff at http://www.vintagepowerwagons.com/ who have been willing to take some time to guide me with parts choices based on their experience. Information like what things wear and should be periodically replaced was very helpful.

Parts breakdown (prices are rounded, some minor items omitted, ask VPW for recommendations):

PartNotesCost
CrankshaftOnly required if broken or out of spec, difficult to get, shipping very expensive$550
Manifold assemblyMine was cracked, I got a coated replacement$500
Fuel line setComplete set with armor springs$400
Carburetor$300
Oil pump$300
Valve tappets (12)$300
Flywheel assembly$75
Fuel pump$200
Motor MountsRubber was aging on mine$100
Spark plug set and wires$75
Crankshaft pulleyMine had a dent$60
Timing chain$90
Oil hose setI opted to replace all rubber parts$40
Water pumpMine was ok but replaced anyway$100
Ignition coil$50
Piston ring set$100
Pistons (6)One of mine split$200
CamshaftFuel pump track was gouged on mine$150
Piston pin bushing set$50
Timing gears, camshaft$70
Timing gears, crankshaft$50
Valve seats and intake valves (6)$150
Distributor rebuildVintage Power Wagons performs this service$350
Valve seats and exhaust valves (6)Machine shop found these
Camshaft bearings$50
Valve guides (12)$60
Clutch kithttps://dcmclassics.com/clutch-components/496-cc-306-complete-package-clutch-disc-pressure-plate-throw-out.html – 10″
From DCM Classics
Would have been on backorder for awhile with other vendors
$350
Engine gasket setMachine shop found these
Rear main seal (neoprene)Machine shop found these
Crankshaft bearing setMachine shop found these
Connecting rod bearing setMachine shop found these
U-Joint set$230
Flange bolts for U-joints$75
Tie rod ends (2) and repair kits$120
Drag link repair kit$140
Idler arm shaft and bushing$35
Drag link dust covers (3)$75
Steering armOriginal ball joint was worn, you can’t replace the ball on the original, VPW had a rebuilt original for a good price. I had an idler arm that came with the truck $50
Brake Line Set (steel w spring protector)Vintage Power Wagons sells a complete set of brake lines. Getting under the vehicle showed some corrosion on the lines and the brake light switch section was falling apart so decided to just replace everything$250
Brake light switch set (Packard)Packard connectors seem to be more stable than the original shell types$50
Radiator RecoreDone at B & D Radiator Shop in McLouth KS. Last army depot went bananas with solder so B&D cleaned that up and recored it since this old radiator was devolving pinholes.$700
Transmission rebuildDone at Smith Brothers, Topeka http://www.smithbrotherstransmission.com/ – Took a bit to find a shop interested in this transmission, was happy to find a shop that seemed genuinely interested in getting this old truck back in motion$2000
Machine ShopDone at NAPA North Topeka http://www.napaonline.com/en/ks/topeka/store/27344/ very helpful machinists there, have been very detailed$5500
MechanicRetired mechanic with good reputation and familiarity with Dodge Power WagonsPending, estimate 3-4k
TotalPending, $12-16k?

Parts are still available but getting difficult to find. None of this has been fast, or cheap. I was able to save money on shipping by picking up the parts, Vintage Power Wagons is only about 4 hours away. My initial guess as to what this might cost was very wrong, it is about double triple what I thought it might be. Once I have final numbers, I’ll provide rounded figures in case someone has the same question I had about scale of pricing for a Dodge M37 engine/transmission rebuild.

M101 Trailer Service Brakes (early type)

M37 and M101

Finding parts for early versions of equipment has been a challenge. Improvements to equipment results in the old part being removed from inventory and the new parts being stocked. For my M101 made in 1953 (coincidentally the same year as the truck) it did not come with service brake levers, and it appears they were removed quite a long time ago. The previous owner had purchased M101 levers, but they are the newer improved type, and the bracket did not fit, and even if it did would not engage the brake cable correctly.

After some extensive research I found the brake lever type and a source for the handles, but not the brackets they mount to. I got the handles from http://powderriverordnance.com – who has an interesting selection of parts and manuals. The brackets simply couldn’t be found, but I asked a local machine shop if they could make one from photos and the trailer and they stated they could. The staff at http://meridenmachineshop.com / http://www.randsmaintenance.com were very helpful and did a very high quality job making and fitting the parts.

M101 Trailer, early style, brake levers installed

I’ll have to adjust the brakes now, since the cables aren’t set, and then test it, but I know the levers on the drums work from when I serviced the wheel hubs and the levers/cables work so I just have to tension them appropriately now. Once that it done, I can park and disconnect this trailer safely without fear of it rolling away. I have read that these levers tend to pinch your hand, which may be why they were replaced, so I’ll have to wear gloves when operating them which isn’t really a bad idea in any case when disconnecting the trailer.

I have the later style M101 brake levers if someone needs that type, I cannot use them with my setup.

M101 later style brake levers

A roundabout way to fix a rear main oil seal leak

is to blow the engine. After nearly 70 years, the engine finally gave up, breaking the crankshaft and breaking a piston. Fortunately, the block appears to be ok.

M37 Crankshaft

Since this is a major repair, I am going to take this opportunity to replace all worn parts in the engine and transmission, hopefully getting another 70 years out of it. Ill detail the costs and parts list associated with this in case anyone is considering a major overhaul for their M37.

This engine lacked power but started and ran well for about 750 miles that I drove it. It suddenly started making a loud clunking sound on a trip which caused me to shut it off and start looking for a way to get it repaired.

At least when it’s done I should resolve that rear main oil leak that has been bugging me.

M37 Cooling system maintenance

After completing this project my truck went from having a variable, but not overheated temp, to stable. The heater works too, just in time for summer. I don’t think I will use acid routinely, but it seemed very effective for use every few years. The procedure I used is below.

TM 9-2320-212-20

9/16 in wrench(s)

1/2 in wrench(s)

Screwdrivers

Water distribution tube

Thermostat gasket (there are two, the housing base gasket, and the top of the thermostat has one inside the thermostat housing)

Bypass elbow gasket

Water pump gasket

Hoses/Belt if you need to replace those, I did in this project

2 ½ -5 lb Oxalic acid (2 ½ lb per flush)

2 ½ lb Washing soda (sodium carbonate)

2 ½ lb Borax

1.  Drain the coolant using the drain cocks – Open the one on the front of the radiator first, to capture as much coolant as possible to reuse or dispose of properly.  After its clear, open the drain on the engine block (near the oil filler tube) to finish.  The drain cock on the engine block was jammed up with gunk on my vehicle, I had to lance it (gently) a few times with stiff wire to get it to drain.  You can remove the whole drain cock with a 9/16 wrench to increase flow or clear obstructions.

I recovered the coolant, filtering it through a colander/tee shirt since it is less than a year old.  Letting it sit a few hours/overnight lets anything not coolant settle to the bottom to be discarded.

2.  Remove the thermostat – This will ensure that any flush cycles through the system without obstruction and is straightforward to do, 2 9/16ths bolts are what holds it on.  It takes some maneuvering to remove without gouging the thermostat, TM -20 page 2-118 illustrates this well, removing the bypass elbow simultaneously makes this easier if you have the gasket.  For the flush cycles, I reused the old gaskets since minor leaks wont matter at this point.

3.  Water Flush – I used a garden hose and set the flow to match the drain rate with the drain cock on the radiator removed, then ran the engine while closely monitoring to ensure the water level stayed full.  This forces water to move through the system and exit the bottom of the radiator.  I also alternated between radiator drain cock and block drain cock, but did not have the engine running while the block drain cock was open.  I did this for about 10 minutes.

4.  Acid Flush – I mixed 1 cup (about 8oz) of oxalic acid per gallon, and the cooling system capacity is 4.25 gallon – I mixed 4 gallons of this solution.  The TM -20 page 2-116 mentions both aluminum chloride and oxalic acid, I could not find a source of aluminum chloride, nor a reference for its use in corrosion removal.  I did find several references to oxalic acid in cooling system maintenance, so I used it by itself.  I did 2 cycles of acid flush, driving the vehicle both times to bring up to running temp.  Both cycles came out florescent green (much like antifreeze) which appears to be the color of rust dissolved in oxalic acid (ferric oxalate) – Cleaning with Oxalic Acid? Here’s What You Need to Know. – CORECHEM Inc.All About Ferric Oxalate (bostick-sullivan.com)

5.  Water flush – same as 3

6.  Soap flush – same as 3 but with detergent (laundry or dishwasher to reduce suds).  Not mentioned in the TM, but I have read several internet references on this and I imagine it would be beneficial to remove any oils that somehow remained after the above.

7. Neutralize – Washing soda (sodium carbonate), 8oz per gallon, running to circulate.  The TM mentions Borax as an ‘inhibitor’, which I will use second to last flush before adding coolant when finished.  Borax isn’t particularly PH basic (PH 9), and am not sure why the TM states to use it, but its cheap and more flushing can’t hurt.

8. Water flush – same as 3

9. Disassemble the cooling system – These steps are to get to the coolant distribution tube, which is apparently liable to get clogged and if it does cools unevenly.  Uneven cooling would result in the front cylinder getting adequate cooling and the rear getting less as the water travels down the tube from front to back. 

10.  Remove tension from the belt – My truck gets belt tension from the alternator, loosening the tension bolt permits the belt to slip of the alternator.  Evaluate the belt for replacement, I will replace mine.

11.  Remove the fan – its straightforward, using 4 1/2in bolts, this is illustrated on page 2-121.  The spacer part will fall out as it isn’t attached to the fan or water pump.  Be careful not to gouge the radiator when removing this.

12.  Remove the 6 radiator and fan shroud bolts – The bolts on my truck appear to have wire holes to prevent them from turning when installed, but no wire was installed.  I used thin boards to support and cushion the radiator when it came loose as the last bolts were removed.

13.  Remove the radiator hoses – Page 2-115 illustrates this well, there is the inlet and outlet hose/tubes.  Evaluate them for replacement, I will replace mine.

14.  Remove the shroud and radiator – Remove the fan shroud being carful not to gouge the radiator, then remove the radiator.  It is possible to do this solo, but easier to do with two people.

15.  Remove the water pump – there are three 9/16 bolts holding the water pump on, remove these and take off the water pump.

16.  Remove/replace the water distribution tube – behind the water pump is the water distribution tube, remove with a tool from Vintage Power Wagons http://www.vintagepowerwagons.com/ (Part #NTP211), I replaced with the Vintage Power Wagon stainless steel tube Part #CC637432.  I flushed out the empty water distro tube channel using a hose attachment/wand that got me to the rear of the block to flush things out instead of spraying debris further in.

17.  Clean the system surfaces – gasket interfaces, hose connections, and other parts all were thoroughly cleaned (washed and wire wheeled where needed).  I spray painted the fan shroud and tubes with black engine paint, and the radiator body (not cooling tubes) with green paint from Army Jeep Parts – Gillespie Coatings Paint | Military Paint | Army Jeep Parts

Painting for corrosion protection

18.  Flush the radiator – My radiator overflow pipe (the small tube from filler neck to the bottom of the radiator for overflow fluids to exit) had been clogged, causing coolant to spray all over the engine from time to time.  Solving this issue was fairly easy, I used electric fence wire to lance the tube, clear the blockage, then flush it out.  The radiator itself benefited from being able to tilt from side to side, dislodging more debris in the bottom and flushing it out with a hose.  Use caution and don’t batter the radiator while doing this.

19.  Install the radiator and fan shroud – Use thin boards to cushion the radiator as it is placed.  I wired my radiator bolts so they wouldn’t loosen, but it seemed fine without it.  The bolts are drilled for wire, so it seemed like it should be done. I used electric fence wire, which should be durable and not prone to corrosion as it is made to be in the weather. I have no idea if this tie is correct, but I assume it will prevent the bolt from turning.

Safety wire to prevent bolts from loosening

20.  Install water pump – using a thin coat of sealant on both sides of the gasket, replace the water pump and gasket

21.  Put the belt in place

22. Install the fan and fan drive pulley, orchestrating all this is tricky with the space available, but possible with patience.

23.  Tension the belt – Page 2-120 details tensioning the belt, which states 1/2in deflection – “Deflection” seems to be space you can push down on a belt as described here – https://www.bestorq.com/library/techinfo/whytension.pdf.  Ill probably need to use the ruler method described here https://www.acepumps.com/en/index.php?/site/applications/C38/Adjustment as I do not have the specific tools available.

24.  Install the thermostat, inlet/outlet hoses, and heater hoses if you have those. The bypass elbow and thermostat housing have to be installed together, there isn’t enough hose between them to maneuver the thermostat in place otherwise.

25. More flush cycles, Borax then water. Check for leaks and test drive.

26. Fill with distilled water and antifreeze and bring to temp to ensure its mixed well

Completed project

Taking the Truck on an acid trip

With summer around the corner and remembering that the truck got over thermostat temp when under load on hot days, I decided to do some cooling system maintenance. Thermostat is 180f, but the truck would get to 200f or so under load but come back down when cruising or idling. This, from what I am reading, isn’t terrible but I would rather deal with it before it gets me stuck somewhere.

I purchased some parts from the very helpful staff at Vintage Power Wagons https://www.vintagepowerwagons.com/: Coolant distribution tube that goes in the block behind the water pump, a tool to remove the distro tube, a thermostat, and a radiator cap. I also got 5lb of oxalic acid, which the TM mentions, to flush the system.

The plan was to do a couple cycles of oxalic acid, drive it around for a bit each cycle, and let it sit a couple hours each cycle. I made an assumption that doing this first would make the water distro tube removal easier. Oxalic acid isn’t a particularly vigorous acid, but I was cautious with it, using the recommended safety equipment. The cooling system is a little under 5gal, and the mix is about 8oz per gallon which worked out to use the whole 5lb. The Oxalic acid in water was clear when freshly mixed, but it came out green after the flush cycle –

Not antifreeze

The system was flushed thoroughly with water prior to acid flush, and was clear, so the photo above is the result of the oxalic acid flush. A significant amount of solids flushed out as well.

The system then was thoroughly flushed with water running the engine each time to circulate, then neutralized with washing soda.

After the system was flushed, I moved to the water distro tube, which was not as bad as I thought it would be. I had to remove the radiator, the cooling fan, and water pump which I will detail after I confirm this all works.

Water distribution tube channel visible after water pump removal

Having seen a couple videos on waster distro tube removal, I was anticipating a fight to get it out. A youtube channel Watson’s Wagons detailed his experience with removing it here – Dodge M37 Water Distribution Tube Removal – YouTube. My tube, possibly due to the flush, came out without a slide hammer much to my surprise. I was anticipating the tube to have solder and other garbage jammed in the channels based on a couple examples on youtube, and it did. The rebuild depot for these vehicles must have had a mechanic that loved solder. I pulled about 3 fingernail sized chunks of solder out.

The thermostat also appears stuck partially open, so I am glad I got a replacement. It may just be stuck in this position which would explain its very sluggish coming up to temp and may have contributed to it not keeping up with heat in warm weather along with the accumulated corrosion in the system. The ‘new’ thermostat was amusingly made in 1966 but looks as good as it did when it was made.

Old thermostat on left, new on right

When it’s complete and confirmed working, ill detail the steps I took but at this point the oxalic acid flush seems very effective at removing corrosion and restoring flow to the cooling system.

March 2022 Parks on the Air (POTA)

Given a long weekend, what better thing to do but camp and get on a radio? I selected Shawnee State Fishing Lake near Topeka, KS since it is open year-round like Nebo. Winter field day in January was chilly, but fairly nice, but this trip really tested the gear. High winds the first day and snow the second into the third.

High winds batter the setup the first day
Hail, followed by snow day two and three

This trip I was able to make the highest number of contacts since starting POTA, with over 150 in a day, plus several ‘Park to Park’ contacts where contact is made with other people at POTA parks. I am getting more efficient at copying/logging, but I also had help from my son who joined me for this trip.

Operating the station

Getting out of the park would have been tough in a regular vehicle, there are some steep inclines and I had to put the truck in 4WD. Once I did, it easily got through the mud and snow.

When the weather gets warmer, I do want to detail the DX Commander antenna while making some improvements to it. It managed the high winds well and, as always, got good reach on the air. I also want to detail some work on the M37, bearing maintenance, brakes, and cooling system as I service those items for 2022. I also need to find some way of adapting or making an antenna for the truck itself on VHF Amateur radio that looks similar to the military antenna on it now.

Winter Field Day 2022

The weather couldn’t have been better with mid 40s in the daytime at Nebo State Fishing Lake, the location for our WFD22 camp. Amusingly, our first contact was someone very close to us, in the vicinity of Holton, KS and we likely picked them up on groundwave. We spent the majority of the time hunting people calling CQ, which slowed us down considerably, but we made around 80 contacts in this way. The M37 and trailer worked beautifully, fresh out of the garage after servicing all 6 wheel hubs. My two sons joined us for a bit and operated a couple contacts, and a fellow amateur operator joined for the whole trip.

WFD22 Camp at Nebo State Fishing Lake

My Duracell Gel lead acid batteries are shot so we had to use the generator (a Honda eu2200i) on this trip, but it did not cause interference and it is very quiet. I am pretty disappointed with the Duracells, I will have to try LiFePo (Lithium Iron Phosphate) batteries at some point. I am very happy with the generator, very easy to maintain and appears to be very reliable.

I also continue to be very happy with the DX Commander antenna, very easy to setup and it has proven to be rugged. I can easily set it up solo but having help of course is welcome. I cut the elements for data frequencies, so I did use a tuner for voice operations, but it didn’t seem to hurt performance.

DX Commander on the lake levy

I really enjoy the WFD events and camping next to the frozen lake made for some beautiful scenery. Our score won’t be spectacular, but just getting out to a campsite and enjoying operating radio made the trip a lot of fun. Next field day, we will likely try incorporating another radio and antenna and try to double up our throughput, likely one data and one voice station.

Military vehicle blackout drive

One aspect of owning a military vehicle that I find fascinating is the parts you can get. Termed “New Old Stock”, meaning parts that have never been used, but are made several decades ago. I ordered a blackout headlight from Kaiser Willys (https://www.kaiserwillys.com) and received a part made in WWII – September 1944 assuming I am reading the stamp correctly.

Headlight from WWII

Of course I do not anticipate driving in blackout drive often or at all, but I do like for the truck systems to all be working if I can fix them.

When I was on active duty in the 80s-90s I often had to drive in blackout as the doctrine at the time was to operate exclusively at night as we had superiority in night vision. While that may have been true, not everyone had goggles and I spent the majority of time driving with the tiny of sliver of light these blackout headlights provide. While it works, it requires a great deal of attention and is fairly nerve racking to do. If you are hiding from aircraft, however, it is very effective at reducing how noticeable you are compared with normal headlights. It was the late 90s since I last saw any unit attempt convoy training at night on any large scale.

This blackout headlight style is an older type, and I am not sure what originally came with a factory M37, but the housing I have fits this type of lamp. The light that came with my truck was dim, and the unit was rusted through. These types of headlights are sealed units, the bulb cannot (easily) be replaced, the bulb and outer glass is press fit into the housing meaning the whole thing is replaced normally.

Since my original was rusted through and mostly ruined anyway, I forced the housing apart with a screwdriver and will see if I can adapt some 12v LED in the housing at some point later if the bulbs become difficult to get.

The bulbs are 6v, and the original M37s were 24v, but mine has been converted to 12v. There was a resistor on the old lamp to reduce the voltage from 12v to 6v, which is common, but may have been the cause for the lamp to be dim. I decided to get a small DC-DC buck converter (https://www.walmart.com/ip/12V-to-6V-2-5A-Step-Down-Waterproof-Miniature-DC-DC-Converter-Power-Supply-Module/924106529?wmlspartner=wlpa&selectedSellerId=101028229) to power the replacement lamp.

Testing buck converter

With the buck converter the lamp appears as bright as I remember them being from my time on active duty. The buck converter easily fits in the blackout headlight housing, even after putting some padding on it. If I ever have an occasion to use the blackout drive, it will at least be serviceable.

View from drivers seat